Conserving Energy Using Analytical Techniques while Protecting the Environment:
Hydrolizer and stripper are employed at various
ammonia-urea complexes to treat contaminated condensates consisting of
seal tank water, seal and flushing water of carbamate and ammonia
pumps, and ammonia unit waste stream from CO2 regenerator overhead
condenser system. Steam is used for hydrolyzing as well as stripping
off NH3 from the hydrolyzed condensate. The use of this steam on urea
unit is not uncommon but utilizing it on ammonia unit, especially as
process steam, has been a skeptical speculation based on the fact that
ammonia unit houses catalytic systems, very sensitive to contaminated
streams. In addition to contaminants like chlorides and sulphates,
presence of ammonia in this steam is also undesirable for the
downstream system. However, the incentive for this utilization is
large, based on tremendous amount of energy saving. Such an incentive
was taken back in 1998 when this steam was taken as process steam.
However, due to unavailability of any sensitive detection equipment,
Low Temperature Shift converter catalyst was de-activated before its
predicted life and the steam was then off lined. This highlighted the
fact that if hydrolizer stripper steam is to be utilized as part of
ammonia unit process steam; careful monitoring and checks of sensitive
nature will have to be conducted because although the incentive is
high, the risks involved are also tremendous. Availability of Ion
Chromatograph, capable of detecting presence of ions in parts per
billion, and careful periodic monitoring of reactor profiles has
resulted in utilization of hydrolizer/ stripper steam as process steam
on ammonia unit again, minimizing hazard to the downstream catalysts
and resulting in saving $ 0.55 million/year.
History of Engro Chemicals:
Engro’s ammonia /urea site was established in 1968
as ESSO Pakistan Fertilizer Company Limited with an annual urea
production capacity of 173,000 tons and a market share of 80 %. The
company was later re-named Exxon Chemical Pakistan Limited (ECPL). By
1988, Exxon Chemical had attained an annual urea production capacity of
268,000 tons through a series of de-bottlenecking steps over the
years. However, the continuous
addition of large capacity plants by competitors had eroded
company’s market share to only 15%.
In this context, ECPL carried out an unprecedented relocation of mothballed ammonia and urea plants in 1992. The ammonia unit was relocated from Pascagoula, Mississippi, USA, while urea unit was relocated from Billingham, UK. The relocation occurred after, as part of their global strategy, Exxon divested from Exxon Chemical Pakistan Limited and the company under the employee-led buy out was renamed as Engro Chemical Pakistan Limited. As a result of the commissioning of relocated plants in 1993, the site annual urea capacity increased to 600,000 tons per annum.
In 1998, the company undertook yet another debottlenecking step “ECES-850 (Engro Conservation & Expansion Step) to improve energy efficiency and increase plant capacity to 850 KT per annum urea. Further steps for service and capacity factor improvement, enabled to produce 950 KT in year 2003.
In this context, ECPL carried out an unprecedented relocation of mothballed ammonia and urea plants in 1992. The ammonia unit was relocated from Pascagoula, Mississippi, USA, while urea unit was relocated from Billingham, UK. The relocation occurred after, as part of their global strategy, Exxon divested from Exxon Chemical Pakistan Limited and the company under the employee-led buy out was renamed as Engro Chemical Pakistan Limited. As a result of the commissioning of relocated plants in 1993, the site annual urea capacity increased to 600,000 tons per annum.
In 1998, the company undertook yet another debottlenecking step “ECES-850 (Engro Conservation & Expansion Step) to improve energy efficiency and increase plant capacity to 850 KT per annum urea. Further steps for service and capacity factor improvement, enabled to produce 950 KT in year 2003.
Introduction:
Cost of steam generation on an ammonia plant is a
typical area of concern, more so lately because of increased gas
prices. Steam saving is, therefore, an area much concentrated upon and
any step in this direction is of importance.
Utilization of hydrolizer and stripper steam as ammonia process steam has had major impact on overall steam saving at the ammonia plant in Engro Chemical Pakistan Ltd.
Utilization of hydrolizer and stripper steam as ammonia process steam has had major impact on overall steam saving at the ammonia plant in Engro Chemical Pakistan Ltd.
Figure1: Process Flow Diagram of hydrolizer stripper unit and its steam path; the dotted lines show steam.
Engro Chemical Pakistan Ltd operates 2700 MTPD urea
plants. The waste water generation from these plants is treated in
hydrolizer and stripper unit where urea is hydrolyzed to give CO2 and
H2O. In addition to the wastewater from urea units, the hydrolizer
stripper also treats waste stream from CO2 regenerator overhead
condenser
system. The hydrolyzed stream is then taken to the stripper where NH3 is stripped off using 6100 kN/m2 (gage) steam and the ammonia free condensate is sent to the lime-softening unit. The steam used for hydrolyzing is the steam that is coming from stripper after stripping. This steam is usually vented or utilized at Urea plants. However, at ECPL this has been used at ammonia unit as process steam.
system. The hydrolyzed stream is then taken to the stripper where NH3 is stripped off using 6100 kN/m2 (gage) steam and the ammonia free condensate is sent to the lime-softening unit. The steam used for hydrolyzing is the steam that is coming from stripper after stripping. This steam is usually vented or utilized at Urea plants. However, at ECPL this has been used at ammonia unit as process steam.
Hydrolizer treats two streams, seal water from urea
unit and CO2 condensate from ammonia unit. Total is 30 m3/hr of
condensate containing 1.2% ammonia and 0.8% urea. About 9 MeT/hr of
steam containing 5-6% ammonia was being vented in the atmosphere at a
height of 30.5 m.
This paper covers the experience of introducing
hydrolizer stripper exit steam as process steam at ammonia unit that
helped to improve the environment and site energy index. Initially, the
activity failed due to fast deactivation and loss of Pre-reformer and
LTS catalyst life. Miscellaneous problem and the subsequent remedial
actions taken to save the catalyst and Cu/Ni exchangers have been
discussed in detail with actual data.
Benefits
Following benefits were gained after the implementation of this project.
- Utilization of hydrolizer stripper steam as ammonia unit process steam improved the energy index of the site. Energy saving of 209 Joules per MeT of Urea was realized.
- Localized pollution in the area due to venting of NH3 rich steam at lower height was addressed after the project.
- Previously, when hydrolizer stripper steam was being vented, cooling tower pH was observed to increase. After this project, this issue has been taken care of.
- Utilization of hydrolizer stripper steam as ammonia unit process steam improved the energy index of the site. Energy saving of 209 Joules per MeT of Urea was realized.
- Localized pollution in the area due to venting of NH3 rich steam at lower height was addressed after the project.
- Previously, when hydrolizer stripper steam was being vented, cooling tower pH was observed to increase. After this project, this issue has been taken care of.
Vulnerabilities Associated with Use of Hydrolizer/ Stripper Steam as Process Steam
Use of hydrolizer and stripper steam as process steam has several vulnerabilities associated with it that are explained in the following.Presence of sulphates and chlorides:
Hydrolizer/ stripper steam has the possibility of
containing chlorides and sulphates in it. Several cooling water
exchangers are installed both on urea units and ammonia unit, in the
process, for cooling the streams before knocking off condensate from
them. These condensates are then treated in the hydrolizer stripper
unit. If the exchangers happen to have any leakages chlorides and
sulphates escape into the system condensates. These ions can be
detrimental to the process in the following ways:
- High sulphate level in the process steam reduces
pre reformer catalyst life although to a lesser extent than hydrogen
sulphide or organic sulphur compounds that may slip from the
desulphurizer.
- Low temperature shift converter catalyst is sensitive to chloride poisoning. Unchecked exposure of the catalyst to chlorides can result in permanent loss of catalyst activity.
- Low temperature shift converter catalyst is sensitive to chloride poisoning. Unchecked exposure of the catalyst to chlorides can result in permanent loss of catalyst activity.
High Ammonia Levels in Process Condensate
Steam from hydrolizer stripper has the potential of
increasing ammonia level in the condensate from carbon dioxide stream as
well as other process streams.
Previous Experience with Hydrolizer Stripper Steam as Process Steam
Hydrolizer stripper steam was lined up with the
process in 1998 for the first time. However, following problems arose
due to which the steam was backed off and vented.
Poisoning of LTSC Catalyst
A cooling water exchanger for carbon dioxide was
leaking due to which chlorides were creeping into the process
condensate. This condensate was lined up to hydrolizer stripper and
hence chlorides were entering the process via hydrolizer/ stripper
steam. LTSC catalyst was exhausted before its due time.
LTSC reaction profile curves at various bed depths
during the period of rapid deactivation are illustrated in Fig. 2. As
illustrated in the figure reaction at 64% bed depth reduced by 7%
during a period of less than a month when chlorides were entering with
the system along with hydrolizer stripper steam.
At the same time reaction at 75% bed depth showed an increase indicating that reaction had shifted lower into the bed.
The lower curve is percentage reaction at 64% bed depth while the upper curve is reaction at 75% bed depth.
The lower curve is percentage reaction at 64% bed depth while the upper curve is reaction at 75% bed depth.
Deactivation of Pre Reformer Catalyst
Faster deactivation of pre-reformer catalyst was also
experienced during the time hydrolizer stripper steam was lined up
with the process. Although the catalyst did not exhaust at that time
and was changed several months later, however, the rate of deactivation
was more pronounced than the normal deactivation rate.
Reaction profiles of pre reformer at 18% and 47% bed depths during the time hydrolizer stripper steam was lined up and sulphates were in the system due to exchanger leakage are shown in Fig 3.
Reaction profiles of pre reformer at 18% and 47% bed depths during the time hydrolizer stripper steam was lined up and sulphates were in the system due to exchanger leakage are shown in Fig 3.
As can be seen from the curves, reaction has dropped
lower into the bed rapidly indicating fast deactivation during a period
of about one month. Upper curve indicates reaction at 18% bed depth
while lower curve indicates reaction at 47% bed depth.
Ammonia in CO2 and Enhanced Corrosion of Cu-Ni Exchangers
Before carrying out this venture, it was generally
believed that due to high temperature any ammonia present in the
process is broken down into hydrogen and nitrogen in secondary
reformer. However, this did not happen in actual experience where
increased ammonia levels were experienced in process condensates
indicating high ammonia level in the process.
Increased ammonia level in process resulted in
presence of ammonia in CO2
stream going to the urea units. Urea units had Cu-Ni exchangers
as inter stage coolers of the CO2 compressor and increased ammonia
caused corrosion of these exchangers. Corrosion was detected by
observed leakage in these exchangers.
Based on these issues, hydrolizer stripper steam was off-lined from the process.Improvements
The incentive for steam saving remained high and
resulted in devising strategies to carry out the venture again but with
improved monitoring techniques and controls.
Ion Chromatographer
The availability of ion chromatographer solved the problem of deficiency in monitoring techniques. Ion chromatographer can detect presence of ions in levels as low as parts per billion. The chromatographer is based on conductivity principle and provided with conductivity suppressor module. It can detect a number of ions in the form of conductivity peaks and can be used for the quantitative as well as qualitative measurement of various anions.Previously, LTSC catalyst was poisoned due to unavailability of monitoring technique capable of measuring minuscule chloride and sulphate levels. Due to this blind spot, chlorides escaped unnoticed into the system and caused poisoning of LTSC. With the ion chromatographer and an efficient monitoring schedule in place, no unnoticed contaminants can enter the system. As soon as any contaminant beyond its acceptable level is detected, hydrolizer stripper steam is off lined from the process and the problem is trouble-shooted and rectified. Steam is not lined up to the process again unless the contaminant levels return to their acceptable limits.
Replacement of Cu-Ni Exchangers
Replacement of Cu-Ni exchangers at urea plants with
stainless steel ones has reduced the vulnerability associated with
increase in ammonia levels.
More Areas of Concern:
Possibility of Carbamate Formation
Introducing the hydrolizer stripper steam into the
system as process steam increases the overall ammonia level in the
process condensates. Increased ammonia in the process stream, as
discussed above, has the potential of being carried over with CO2 to
urea units. It has been experienced in two instances, specially during
plant start up, that when waste water containing higher than normal
operating concentration of ammonia has been lined up with hydrolizer
stripper, ammonia concentration has increased in hydrolizer/ stripper
steam with subsequent increase in ammonia concentration in CO2.
Presence of ammonia in CO2 has resulted in carbamate formation in CO2
compressor valves.
However, presence of ammonia alone cannot cause
carbamate formation. Water should also be present in addition to
favorable temperature and pressure. Following steps have been taken
to check the formation of carbamate:
- Ensuring the absence of water in CO2 stream. This means making sure no knock out drum after CO2 compressor inter stage coolers is malfunctioning.
- Carrying out regular monitoring of process condensates at ammonia unit for presence of ammonia. Increased ammonia in process condensates is usually a harbinger of presence of ammonia in CO2.
- Based on these close checks, increased ammonia in process streams is handled and hydrolizer/ stripper steam off-lined from process in case of increase beyond acceptable levels.
- Ensuring the absence of water in CO2 stream. This means making sure no knock out drum after CO2 compressor inter stage coolers is malfunctioning.
- Carrying out regular monitoring of process condensates at ammonia unit for presence of ammonia. Increased ammonia in process condensates is usually a harbinger of presence of ammonia in CO2.
- Based on these close checks, increased ammonia in process streams is handled and hydrolizer/ stripper steam off-lined from process in case of increase beyond acceptable levels.
Conclusion
Industrial units usually incur large expenses
operating an environmental improvement project that are justified only
by the improvement in environmental standards being practiced by the
industry. However, utilization of hydrolizer stripper steam in the
process has given a new dimension to this project as it has ended up
causing savings worth millions of dollars in addition to being a
necessity for effluent treatment. Another associated benefit has been
elimination of localized air pollution.
The essence of the whole project, however, lies in improved monitoring techniques and stringent monitoring standards without which it can cause damage to the process far exceeding its benefit. It is a perfect example of how good analysis and monitoring techniques can cause conservation of energy and improvement of energy indices.
The essence of the whole project, however, lies in improved monitoring techniques and stringent monitoring standards without which it can cause damage to the process far exceeding its benefit. It is a perfect example of how good analysis and monitoring techniques can cause conservation of energy and improvement of energy indices.
Jahangir Waheed
Jahangir Waheed has 24 years of experience in fertilizer industry. He is currently working as Technical Manager, at Engro Fertilizers Limited, Pakistan |
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